Well, I was going to work and had the girl running around 70 and it sputtered a little and then cut off, looks down at the temp. Gauge and it was pegged out. Pulled over and pop the hood and see what was left of the coolant and oil all over the motor. It is a B3 auto. I know the head is bad now but what ells do yall think is bad now?
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Was running good and then....
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I say its time for a motor swap. Probably will be cheaper in the long run too. Head could be warped. Who knows what kind of damage it did to your bearings. If you did blow the headgasket be sure to strip that motor down asap and get all the water out of it if you plan on saving it. All in all I would swap motors or find a stock replacement.
Has caught the most Festivas on Fire on this board!!
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Drop in a BP
1988 323 Station Wagon - KLG4 swapped
1988 323 GT - B6T Powered
2008 Ford Escape - Rollover Survivor
1990 Festiva - First Ever Completed KLZE swap (SOLD)
If no one from the future stops you from doing it, how bad of a decision can it really be?
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Couldn't you hear any problem with the running of the engine before it totally failed? Were you listening to the radio? Bad muffler? Just curious.
John Gunn
Coronado, CAJohn Gunn
Coronado, CA
Improving anything
Improves everything. Copyright 2011 John Gunn
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