PHEW! False alarm... I reached under there and did the jumper on the neutral safety switch and it still wouldn't start. That is when I noticed a thicker gauge black wire sticking out of the harness that is right there. It had clearly been cut by a former owner (I'm thinking it was a disconnect for either a remote start, or like an engine kill for an alarm.) The wire had about 6" of non-matching wire butt connected on each end. One of the butt connectors had come off. I looked up and saw and thought "No... Freaking... Way..." touched them together and it started right up. Runs better than it has in a month.
Thanks for the help guys!
Thanks for the help guys!
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